uservdwlkr
Battery issues - all pulls are following a battery replacement, some lean codes, and a jumpy AFR. 1 pull is before discovering my amplifier ground was not connected for a week, the other 2 are after.
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03/31/2024
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Codes popped up shortly following battery complete death & replacement.
Active codes: 2BC0 Mixture control, fuel air mixture too lean - 36FD DME main relay, plausibility, prematurely dropped out - 387C Power management, battery total discharge (cleared and shouldn't come back) - 3887 vehicle voltage, working area: voltage too low (cleared and shouldn't come back)
Shadow codes: 2C42 Mixture control, multiple fault - 2D45 Valvetronic, adjustment range, stop not taught in due to ambient conditions
Notes: Driving, I can see small spikes in the AFR from 14.7 to 16.2 occasionally at bumper-to-bumper traffic speeds. WOT pulls hard initially, but felt like it tapered off weirdly - which is evident in the low peak boost numbers. On other logs I hit 18PSI, but typically I see 21 at max. Idle feels good, WOT just feels a little weak on the upper-range, slow driving is intermittently sluggish and choppy.
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03/14/2024
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09/15/2021
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09/09/2021
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09/09/2021
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