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Added November 19, 2021 by jpearcedatazap
boost not coming up, i don't believe there is a boost leak. there is an odd thing where after going wot for a few second and lifting all the way off, it will still keep the throttle position open for a beat longer. I already did a compression test months ago and all good, but didn't do a leak down until now. so did it and all cylinders are good, largest leak was 3%. with my limited knowledge of the operation of this DME, it seem there is a wastegate control issue. i am confident all the vacuum lines are good (as i just replaced them and and did a leak test at each connection point) but is there a method of testing the system and observing function? also checked spark plug gap while testing leak down and all were either .021" or .022" with the two steps cooler.
  • 91 Octane
boost not coming up, i don't believe there is a boost leak. there is an odd thing where after going wot for a few second and lifting all the way off, it will still keep the throttle position open for a beat longer. I already did a compression test months ago and all good, but didn't do a leak down until now. so did it and all cylinders are good, largest leak was 3%. with my limited knowledge of the operation of this DME, it seem there is a wastegate control issue. i am confident all the vacuum lines are good (as i just replaced them and and did a leak test at each connection point) but is there a method of testing the system and observing function? also checked spark plug gap while testing leak down and all were either .021" or .022" with the two steps cooler.
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