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userhypertrophy07
08/31/2016
BQ91 ATP IKC0S IS v1 3rd gear pull Kevin Brown
P2AAF, Fuel pump, plausibilty I was having this same issue on the E30 map as well, I assumed because I wasn't blending with 91, only used 100% E85 instead. But now same code has popped up. Feels like the clutch is slipping not sure what the issue is. I don't think I'm running rich anymore?
  • 91 Octane
08/31/2016
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08/28/2016
BQ91 IKC0S IS base 3rd gear pull Kevin Brown
Mods: Stock airbox (K&N iair filter) Wagner 7inch FMIC chargepipe ram air 3 inch catless dp full catless exhaust fuel it stg2 lpfp turbo smart diverter valves toyo r888 tires ngk laser iridium spark plugs
  • 91 Octane
08/28/2016
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07/17/2016
BQE30 IKC0S IS v13 3rd gear pull Kevin Brown
Targeted E85 now I went doors with a 818whp procharged mustang tonight!
  • e85
07/17/2016
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07/16/2016
BQE30 IKC0S IS v12 3rd gear pull Kevin Brown
WOT all night then all of a sudden CEL came on. I plugged in my Cobb AP and got the following codes: P30FE Boost control, boost pressure too high error wastegate 1-clamped, P3100 Limpmode There has been a terrible rattle the past couple weeks. I assumed it was the exhaust but it may be the wastegate like you said before. I did these logs about n hour after the CEL came on.
  • e50
07/16/2016
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07/09/2016
BQE30 IKC0S IS v12 4th gear dyno pull Kevin Brown
Targeted E50 Approx 100°F outside 434whp/517wtq
  • e50
07/09/2016
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