Same problems occurred in both logs.
Acts differently.
Sometimes boost switches off during pull, sometimes it switches off after pull.
F.E - during pull - OK - after pull, if you do pull again, boost is cut.
CEL ON - No Drivetrain Malfunction.
Tried 38psi target. 35Psi actual. Adjusted with wg position but problem was same. (Tried just to make little deviation to not be near overboost area.)